| Title | PRODUCTIVITY ANALYSIS AND OPTIMIZATION OF WELL SK-2D MINDANAO I GEOTHERMAL PROJECT, PHILIPPINES |
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| Authors | P.O. Molina, R.C.M. Malate, B.C. Buiiing, D.M. Yglopaz, J.J.C. Austria, A.M. Lacanilao |
| Year | 1998 |
| Conference | Stanford Geothermal Workshop |
| Keywords | Mt. Apo, Philippines |
| Abstract | Well intervention through casing perforation and acid treatment was performed on well SK-2D to improve its productivity. Completion tests indicated stimulation of the mud-damaged payzones, althoughinitial discharge tests showed that contribution froin the stimulated bottom zone was masking the potential two-phase feed from tlie upper perforatedintervals.Subsequent series of short-term discharge tests suggest recovery of the two-phase upper payzone and remarkable improvement in the output of the well. Wellbore simulation of SK-2D using flowing temperature-pressure-spinner (TPS) logs and discharge data projects possible optimization of well utilization by controlling the bottom liquid feed zone and maximizing the contribution from the upper two-phase zone. |